Black Jack: Wreck. ugh...

New Accufab Throttle Body:
Goodbye, BBK TB. You whistle better than me, but your services will no longer be required.

Swapped a polished (too pretty for Black Jack) Accufab 70mm TB that I picked up for $210 in its place, tonight. The whistle at idle is gone! Unfortunately, it's been replaced by a much worse whistle at about 1/4 throttle. After some quick looking, I think it may be either of the following: 1. improper port-matching with the gaskets, 2. need to smooth the IAC port & perhaps TB blade, though whistling from an Accufab was not supposed to happen.

Could be either issue. I didn't closely check the gasket alignment when I put everything together, & perhaps the gasket shifted into the air stream. I'll pull it apart and check it in the next couple of days. However, 2 is still possible. I noticed when inspecting the TB that the IAC port into the TB has sharp edges and that the blade is roughly in its path at what I'd guess is around 1/4 throttle.

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After pic:
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EGR Delete
I pulled the EGR valve out while I was at it & replaced it with a blocking plate. I didn't like the look at the dirty intake plenum, and I want to clean up the engine bay over there, a bit. I plugged it back in for now & zip tied it behind the upper intake/head on the passenger side. Ultimately, based on a diagram provided in another thread, thanks @AeroCoupe, I'll come back to it to ensure the computer knows the EGR is non-functional, while hopefully refraining from giving a CEL.

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TB spacer/Coolant Line bypass
Finally pulled those hoses off & that rear one was a PITA to scrape off with the little room I had to work with. I ran a new hose, bypassing the EGR spacer completely & it looks a little cleaner in that area, now.

Other Notes:
The TPS settled very nicely in at .95 volts. I tweaked the idle RPM a bit, but 900 on the gauge (who knows how accurate...) is what the car liked. I could get it down to ~750-800 but it would start to surge. At first I took a quick cruise and liked it, but then back to surging & even stalled the engine when I turned on the A/C. First rule of tuning: give the car what it likes! Now, other than the whistling sound, the car is running like a top.

I'm still holding onto the accufab race 70mm TB & may install it one day. It doesn't work with the BBK/MAC intake tract on the car & I don't care to spend hundreds on an aftermarket one, though I might fab up something that will work eventually. In any case, I took the opportunity to nab a pic of them side-by-side:

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Notably, the race TB does not have a crankcase vent tube. Also, you can see how it has more of a chamfered, funnel from a 90mm port down to the 70mm blade. This is kinda useless behind my 75mm bullet MAF, though I might still try it out.

Cleaning the passenger corner of the bay:
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Alright, it's been a while since I've taken this on, but is it as simple as just removing the TAB, TAD, and EGR controller? I have no smog pump, no cats, no EGR ports/tubes in the GT40X cylinder heads, which are plugged. Now, that I've removed the EGR Valve & its dedicated vacuum line from the intake vacuum port, which is capped, can I just remove these 3 gizmos attached to the strut tower? The vaccuum diagram (thanks @jrichker) seems to show me that I need to ensure vacuum runs from the check valve to a splitter that includes the reservoir & HVAC controls. Other than that, seems like I can remove all other vacuum lines without issue.

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On the electrical side, it looks like (thanks, @Mustang5L5) the only thing I need to worry about is the proper EGR resistor. The TAB & TAD will apparently kick a code or two, but won't trip the CEL... fine by me.

Am I missing anything? Cleaning up this side of the engine bay will make room for my adjustable brake prop valve, which should be coming up soon.
 
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Update

Fixed jumpy Cable-X to speedo: The speedo was jumping so hard while stopped and idling that it actually threw the needle out of calibration. Had to pull the Gauge Cluster cover again to correct it. Turned out to be an unstable ground wire to the Dakota signal converter. I've rewired the power & ground to run from the Hvac and to the dash instead of the same circuit that the Reverse Lockout & line-lock are on. Now, it's still a little jumpy up to around 30, which may actually be a bit worse than before, but beyond 30, it stabilizes and runs within 1mph up to 100mph compared to my Garmin & Escort Radar Detector.

Installed Fog light switch: No, I don't have fog lights, but while I had the stuff apart, I went ahead and put it in. This is the first part install towards my nitrous kit. That will be the manual on switch. Will work nicely, because it was already a blank switch on the gauge cluster bezel. I'll have to rewire that to switched power from the stock wiring tie-in to the headlights, which by the way worked when I put the fuse in the right spot, switched the headlights on, and tested voltage to the fog light switch wires.

Eliminated a maddening squeak: Turned out to be the engine bay seal/weatherstrip between the hood and firewall. One of the clips was scraping the firewall ever so slightly and worse than nails on a chalkboard, it was really getting to me.

EGR eliminator plugs arrived: I'll report back on whether they trip the CEL. Look cheaply 3D printed. Will keep an eye on them to make sure it doesn't melt, but I think it'll be fine. Bought 2. I'm sure this won't be the last time I need one & I don't know if we'll keep finding them on the market.
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Looks nice without the EGR hanging off the back, and I'll probably tuck it away and leave it connected, even after what's coming next... Looks better plugged in than having an empty plug.

The future work on Black Jack is starting to add up:

Flexing my tuning muscles again soon:
However, puny they may be... I have a Moates Quarterhorse enroute. Found a guy selling a Moates Quarterhorse, which was the piggyback EEC tuner of choice in that community until they went out of business, I guess, late last year. I wouldn't have popped for the $1k+ PimpXS/TerminatorX... didn't want the PITA of installing a new harness. Like the idea of plugging in a QH on any Fox to assist in diagnosing any glitches/issues for as long as it lasts. It will come with a Binary Editor license, a multi-tune switch, the optional bluetooth adapter, and it's a more recent version with a removeable instead of soldered battery.

Honestly, in terms of driveability, Black Jack is running beautifully at all RPMs, at cruise, in a parking lot, etc... The biggest drivers to have the ability to tune myself are: 1) Rich idle (update injector size & tweak MAF transfer function), 2) fixing timing at idle & cruise: setting base timing to 18*, while optimal at WOT causes unnecessary advance at idle & cruise, 3) EGR off, 4) learning more about the stock strategies & what makes a street car so driveable.

I don't think I'm really going to be doing that much, but then again, I get sucked into stuff like this sometimes. Will probably pony up for EEC Analyzer. Looks cool & fun to use.

MSD Digital 6 Plus enroute, too:
Since my A9L went tits up, I decided to upgrade for:
1) 6,100 rev limiter (keeps it off of the fuel cut 6,250 stock limiter)
2) 3.5k - 4.5k RPM 2-step (street vs. track launching)
3) ~6* timing retard for when I run nitrous (will be a 150 wet shot)

Fix Accufab whistle: I think I just need to hand port the IAC ports in the Throttle Body to smooth the edges.

Brakes, of course: This is not on the back burner. I think I've got all the parts. I'm not super pumped to do the work, but I want to get the Cobra Brakes and 5-lug swap done before Foxtoberfest.
 
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Friday wasn't the most pleasant of car days...

Was on the way home from work, wanted to swing by the military clothing store and decided to take some back roads on post and try to work my way over to the store. It didn't go so well, and I was just about to use that parking lot to turn around when:
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It completely caught me by surprise. I took that first pic from full standing height @ 6'4", and because of a little hill and drop, I just couldn't see the pot hole as I approached. Fortunately, it seems like the tire did a pretty good job protecting the wheel and most of what looks like damage to the wheel in the above pic is really just the rubber of the tire that stayed on the wheel when it got pinched. When I go to 5 lug, the new wheels in the garage are going on, anyways. So, I probably just hurt the resale on these by $100-200.

On the bright side, it looks like tire rack's road hazard warranty is going to cover the tire replacement. The tire's already enroute and should be here Wednesday.

A/C is down:
When I left the gym in the morning after showering, I usually run the A/C full blast to help dry & cool me off before I show up to work a sweaty mess. Well, in response to all the braggin' I've been doin' about the A/C on Stangnet, it decided to straighten me out. I figured out what was up, today. It's really not the car's fault. I thought I'd done a good job insulating this from the heat of the header, but I was wrong. It burned through the header wrap and burned through the aluminum. I guess I'll just have to bend it further away from the header on the next go-round.
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Fortunately, the parts from rock auto are on order for a total of about $70, and I already have the freon and tools at home to vacuum & charge the system. So, everything'll work out in the end.

While the car's down awaiting the tire and A/C stuff, I'm taking a trip to tie up some loose ends back in KY, and I might just let someone do the 5-lug and brake swap while I won't be driving it for a week anyways. I'll ask a couple of shops on Monday, and if they can't do it, I'll probably just end up doing it myself, like I'd planned, anyways. Just hard to find time with so much going on.
 
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Ooh :poo:. Contact the city and see if they’ll cover the damage from the pothole if that ever happens again. Had a friend who had two wheels replaced on his truck when it hit a pothole, all covered by the city.
 
A/C Trials and Tribulations - probably resolved... again:
Well, I just didn't have the patience to wait the 3 weeks all the stores around here were telling me I'd have to leave the car with them. I figured what's the worst I can do? Maybe cost myself more money replacing stuff while learning, perhaps the hard way, about how to do a/c work. Thanks to the Chrisfix youtube video & his equipment list, which I copied, I think I did alright. I replaced the accumulator & the liquid line. Then, I charged the system to 27 oz after I saw one of Jrichker's posts suggesting 26-28oz for R134a. Today was my second day driving the car since the work. It was 97* outside and I couldn't get the a/c to blow colder than 60*. I was still comfortable, but pretty concerned that my problems were getting worse.

After some research, I came to the possible conclusion that somehow I'd failed to properly evacuate air/humidity from the system. So, I gave it another go, tonight. After leaving the vacuum pump on the system for ~2 hours, I refilled the system a little more methodically. The lower end of the range from another of Jrichker's posts was 24 oz of R134a for these converted systems. From there I added 1oz at a time all the way to 28.5 oz, because I overshot a little. The temps in the car were good at idle, but the compressor kicked on and off every few seconds. On the test drive, at one point, the temps on the gauge rose again to 56*. Damn...

Came back to the garage and took some notes: the hi-side pressure would slowly rise to 237 psi, and the low-side would drop from 40psi to 20psi on my gauge, at which point the low-pressure switch would cut the compressor. My garage temp reading was 89* with 65% humidity. The reference chart I used called for up to 270 psi @ 90*. So, I decided to say screw it about the recommended system capacity and let's see what it takes to get to the pressure on the chart... Again, the worst thing is that this'll be an expensive learning experience. So, in the name of science, I added and added until I got the high side to read as high as 290 psi. It took me to just over 32oz of R134. I was mostly trying to keep the low-side pressures high enough to keep the compressor going. I stopped there, though. Just wasn't comfortable going to far beyond the high end of recommended.

After 10 or so minutes I took some final readings. Gauge pressure on blower setting 3, max A/C was between the 44 & 48* line on my mechanical gauge. High side pressure would rise to ~285-287 psi while it took the low-side 35-37 seconds to drop from 40 to 20 psi at idle before compressor cutout -- much longer than before. I feel that this is working much better, though I'm not happy about the amount of freon the system took to get there, nor the high side pressures or the low-side cutouts.

At the end of the day, I reasoned that I'd been extremely happy with the car's A/C for so long, previous techs must have just been overcharging the system. My research indicates that there may be a high-side blockage of some kind that would cause slightly excessive hi-side pressures simultaneous to excessively low low-side pressures. However, the most common candidate folks refer to is the orifice tube, which was replaced within the liquid line. The next candidate, I figure, is a blocked condenser itself. But hell, if I'm going to do all of that work, I'll cross that bridge when I come to it, and if I burn out the compressor by overcharging the system in the meantime, I'll cross that one, too. Let's just see how this works out.
 
Is the condenser free of debris in the fins? Literally ran into this on a car when we pulled the motor out of a friend's Coupe. He had the radiator out getting it checked and cleaned so my buddy decided to take the car to the car wash and clean the engine bay. When cleaning it he noticed he could not see through the condenser so he gently sprayed water from the engine side and holy crap the amount of dirt, small rocks, and bugs that came out of that thing was insane. Needless to say the AC worked amazingly well after the motor went back in.
 
The reason why 134a retrofit systems typically recommend a reduced charge is in case there is old oil left in the system and the system is overcharged with oil. Oil cannot be compressed, so essentially you reduce the capacity of the entire system. To compensate, you typically put less refrigerant in. In a brand spanking new system with new components where you are adding new fresh oil into empty parts, you can typically put aside the 80% rule and go with a full charge. Again...the 80% rule was just in case you didn't flush all the added mineral oil out of an R12 system when you added the R134a oil.

If the system has the proper amount of oil in it, you can add close to the factory fill. Really, i charge by weight and pressure. 280psi high side is about where i would expect it at about 90 degrees at the high end of the acceptable range. I wouldn't start worrying until you get up in the 350psi range. The SN95 has a high pressure cutoff in the 400psi range. 134 will have a higher pressure drop across the orifice. You do need to reduce the low pressure cutoff on fox cars. With R12 cars, the low pressure cutoff is 25 psi. With R134 you should drop it to around 20-21psi.

Fox cars do not have a high pressure cutoff. They do have a high pressure relief valve on the compressor. It blows at 450 psi
 
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With regards to reducing the low pressure cut off jrichker lays out in Post #2 here:


Is it really that easy or should a person just buy a cutoff switch for a 94/95 car at a parts store?
 
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There's a schrader valve under the cutoff switch, so you just unscrew the old and screw in the new one. Under the plug, if you look down into the connector you will see a small flat-head screw. You can turn that to adjust the pressure.

You can either swap it out with the SN95 one, or just watch your gauges and make adjustments when the compressor is cycling. Just watch the low side and observe where the compressor clicks off. turning it counterclockwise decreases the pressure. I think jrichker said 1 full turn is about 4 psi.
 
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Just finished up the Cobra brakes, and the pull to the left on initial braking and pull to the right while letting off is gone! The pedal is nicely firm & responsive for normal driving. But, even after bedding the pads & adjusting the prop valve for correct front/rear bias, it takes a ton of pedal effort to get to the braking threshold before lockup... It's too much! My leg would be exhausted on a track day. I think I'll check vacuum & if that looks fine, then I'll convert to the 94 Cobra MC, even with the 93 Cobra booster.

Please help with cruise control:
Biggest problem is the Cruise control no longer works. I've tested continuity in the wiring from the trans through the Dakota converter & back to the point it goes into the wiring harness and everything checks out. Fuses are all good. I noticed the brake lights are just a hair from triggering. Is it possible that the brake switch/signal to turn off the cruise control activates before the brake lights would turn on? Can I pull a fuse or something to eliminate the brake switch from signaling the cruise control to turn off?
 
I'm glad the brakes are better for you now, but I can't say on the cruise control as mine never worked and I never cared. Does the cruise need a vacuum source to work? I feel like it does but don't recall.