- Jan 16, 2014
- 20
- 0
- 2
so I have a 95 GT that I just finished rebuilding the top end with some machined parts and it was all running amazing! well I finally ordered myself the sct 4 bank eliminator from bama performance and threw in my 24 lb injectors to go with the tune that I ordered....well now its running HORRIBLE! it's almost like the spout connector is out or...like the timing is being retarded as the rpms begin to rise. I replaced all my plug wires b/c the #1 wire was broken in two pieces at one end...have an MSD ignition and rotor cap on the stock dizzy. im not sure what it could be other than maybe a crushed lifter due to the higher tension comp cam springs I have on it now, or maybe a broken timing chain. also about 80% of the time the car wont start unless I take the SPOUT connector out...then it fires right up.
to simplify- before tuner was installed(cleaned the computer as per bama instructions with alcohol and scraper) the car would run on a stock tune even with the 24lb injectors;just really rich. after putting in the chip with the tune it runs like the spout connector is disconnected at like 12 degrees advance.
I don't think its the tune though, because it does it even with the chip removed.
as a way to test the spout connector, how would I set it up to run a "lock out" timing? just set the timing at about 23 BTDC with the spout connector out and leave it out?
also I've already followed guides on here on how to restab the dizzy and I did move the rotor one tooth over and It helped slightly.
to simplify- before tuner was installed(cleaned the computer as per bama instructions with alcohol and scraper) the car would run on a stock tune even with the 24lb injectors;just really rich. after putting in the chip with the tune it runs like the spout connector is disconnected at like 12 degrees advance.
I don't think its the tune though, because it does it even with the chip removed.
as a way to test the spout connector, how would I set it up to run a "lock out" timing? just set the timing at about 23 BTDC with the spout connector out and leave it out?
also I've already followed guides on here on how to restab the dizzy and I did move the rotor one tooth over and It helped slightly.