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Kar Kraft faced considerable obstacles in the development of the Boss 429 Mustang, including the fact that the engine bay was over 2 inches too narrow for the motor! This was solved by moving the entire suspension out a full inch on each side. This required new reshaped shock towers, widened strut tower brace, redesigned top and bottom suspension arms, redesigned heavy duty uprights, and heavy duty springs. Also a smaller new power brake booster was needed to clear the big engine valve cover. The battery was placed in the trunk to improve the cars weight distribution; also the cars rear suspension was beefed up with staggered shocks, heavy duty springs, and a thick rear stabilizer bar. The car sat an inch lower overall than a stock Mustang did, so a special "short" front spoiler was designed to fit the clearance available.