I replaced the intake cause the stocker was cracked. Since then it sounds like a WRX. It runs like crap of course. I had the codes pulled and was told it's running lean. Pulling the fuel injector plugs one at a time doesn't really make much of a difference at all. 1 or 2 of them will make it sputter a little then go back to normal. I have checked the spark plug wire routing and that's fine. I haven't had a chance to pull the plugs and look at them. I really don't see what that's gonna tell me, if they ain't working it would be rich not lean. I have checked the injector connectors with a noid light and they all show fine. What else can I check on this stupid thing? I do have a tweecer R/T that I bought for my 94 but beings it's not being used I could hook it up if that will tell me anything. I would really like to get this thing running soon

. I have to keep it under 2k rpm and go slow. I left it running to warm up and checked the torque on the intake which all checked good. Tried to drive it again and still horrible. The heads dried up and I didn't notice any wetness after driving it.