Some of you may have seen my other threads about suspected fuel starvation and delayed starting. I got the new fuel pump in and both issues are now fixed. The car is now running better than it ever has.
Thanks to everyone who posted on my threads to help with things.
I discovered some things along the way. Had a new regulator and pump on hand. I did the pump first and the car started quickly so I knew that issue was solved. But then the car started having a surging idle condition it had never had before. I hooked up a pressure gauge and the idle reading was 80psi. I thought it was the regulator so I changed it too but the pressure was still at 80psi causing idle surge. I eventually discovered that the return line in the engine compartment was kinked because the hose was on top of the steering rack boot instead of hanging down in front of it. Either I did that when I changed the rack or the alignment shop guy did. Who knows but its fixed now.
Furthermore, when I took the old pump out of the tank I found the S hose split open where it connects to the pump. Surely this had to be contributing to the loss of pressure that caused the performance issues.
Altogether I believe the pump was weak and on the way out from the beginning. Then, when my dufus ass, or the alignment shop guy, kinked the return line it caused excessive pressure which split the somewhat dry rotting S hose in the tank. The result was drastic drop in pressure and the performance issues.
Anyway, I have return line fixed and the Kirban regulator adjusted and now its a 39psi vac hose off at idle and 30psi with vac hose connected at idle. It runs frigging great!
Check out this picture of the S hose connection at the old fuel pump.
Thanks to everyone who posted on my threads to help with things.
I discovered some things along the way. Had a new regulator and pump on hand. I did the pump first and the car started quickly so I knew that issue was solved. But then the car started having a surging idle condition it had never had before. I hooked up a pressure gauge and the idle reading was 80psi. I thought it was the regulator so I changed it too but the pressure was still at 80psi causing idle surge. I eventually discovered that the return line in the engine compartment was kinked because the hose was on top of the steering rack boot instead of hanging down in front of it. Either I did that when I changed the rack or the alignment shop guy did. Who knows but its fixed now.
Furthermore, when I took the old pump out of the tank I found the S hose split open where it connects to the pump. Surely this had to be contributing to the loss of pressure that caused the performance issues.
Altogether I believe the pump was weak and on the way out from the beginning. Then, when my dufus ass, or the alignment shop guy, kinked the return line it caused excessive pressure which split the somewhat dry rotting S hose in the tank. The result was drastic drop in pressure and the performance issues.
Anyway, I have return line fixed and the Kirban regulator adjusted and now its a 39psi vac hose off at idle and 30psi with vac hose connected at idle. It runs frigging great!
Check out this picture of the S hose connection at the old fuel pump.