Background--- on my stock factory shortblock with unported gt40 heads, TFS 1 cam, and ported stock lower I ran a 13.5 @102 with a 2.2 60ft. And before that running with the factory long block (stock heads, intake, cam) I ran a 14.3 @ 98.
I had to replace the shortblock due to wear and tear.
I have a D.S.S. 306, forged pistons, ball, ect... the gt40 heads were ported and done by a perfessional, the intake is a ported gt40 intake, and still running the tfs1 cam, The only thing I re-used was the stock lifters (they looked good with not too bad wear) and rockers with the stock length pushrods. The heads are shaved .065 and I should have about 10.5:1 - 11:1 comp. depending on how much matt. makes a diff. when polishing the chambers (removed the casting flash to smooth no re-shaping).
I ran a 14.5 @98 at a local shootout back in April or March...preaty pissed but looked into some things, the #6 and 7 cyl. were not getting fuel. at all, the pass. side bank was rich bad from this.
I found a poor connection (used a noid to test the harness an it got juice) and put some di-elec. grease on the conn. After driving it about 250-300 miles all the plugs have even wear...I fig. there getting fuel...everything should be sorted out.
Tonight I ran 14.1 @99 2.29 60ft ... 14.3 @ 98 2.3 60ft... 15.7 @78 2.2 60ft (missed 4th bigtime)... and 14.3 @98 with a 2.01 60ft.
No matter what I did with the tune changed from 30*total at wot to 32* at wot, from mid 12 a/F to 13.0 a/f.
other than alittle idle issue it drives and gets around perfect, no bucking, stalling, surging, overheating, good mileage, all my datalogs show things are fine in the eec.
I had to replace the shortblock due to wear and tear.
I have a D.S.S. 306, forged pistons, ball, ect... the gt40 heads were ported and done by a perfessional, the intake is a ported gt40 intake, and still running the tfs1 cam, The only thing I re-used was the stock lifters (they looked good with not too bad wear) and rockers with the stock length pushrods. The heads are shaved .065 and I should have about 10.5:1 - 11:1 comp. depending on how much matt. makes a diff. when polishing the chambers (removed the casting flash to smooth no re-shaping).
I ran a 14.5 @98 at a local shootout back in April or March...preaty pissed but looked into some things, the #6 and 7 cyl. were not getting fuel. at all, the pass. side bank was rich bad from this.
I found a poor connection (used a noid to test the harness an it got juice) and put some di-elec. grease on the conn. After driving it about 250-300 miles all the plugs have even wear...I fig. there getting fuel...everything should be sorted out.
Tonight I ran 14.1 @99 2.29 60ft ... 14.3 @ 98 2.3 60ft... 15.7 @78 2.2 60ft (missed 4th bigtime)... and 14.3 @98 with a 2.01 60ft.
No matter what I did with the tune changed from 30*total at wot to 32* at wot, from mid 12 a/F to 13.0 a/f.