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  • 1979 - 1995 (Fox, SN95.0, & 2.3L) -General/Talk-
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LOL..Car is WAY WEAK!!!!

  • Thread starter Thread starter 4Jenna
  • Start date Start date Jul 11, 2004

4Jenna

Founding Member
Sep 12, 2001
4,326
6
69
AZ
Jul 11, 2004
#1
  • Jul 11, 2004
  • #1
Well I drove the car out tonight and noticed it felt REALLY down on power..even for 5psi...
Any how I instantly noticed that the car felt weird and it was obviously a timing thing...exh popping, and the car was running extremely hot...like 200-210 cruising, and with the A/C on the highway 220...I was like OMG A/C off!!!
Anyways I popped the hood and heard a loud ass BUZZ BUZZ every couple seconds....I was like WTF. Then I noticed it was coming from the distributor...whoa...I put my hand on it and could feel the BUZZ BUZZ (pretty loud to) through my hand!
I pulled the cap off and everything looked ok. My distrib has had about a 1/2 x 1/2 piece missing outta the housing (cap goes over it) for awhile...prob should replace...but this is weird....any ideas?
I'm thinking I ****ed the timing up or something since I can't read the balancer anymore from the good ole Fla rust (although I did mark it with #1 TDC...and timed it off that)
But running so hot....weird
Low on power...weird
Buzz Buzz....weird.

Well what'da think
It's to late to mess with it tonight, so I'll sleep on it...lol
 

donjohn

New Member
Feb 7, 2004
1,757
0
0
Irvine - Southern California
Jul 11, 2004
#2
  • Jul 11, 2004
  • #2
well after flying in a freakin jet anything is gonna be low on power. before you said your distributor got eaten up i was gonna say your a/c probalby just needed to be recharged or something but ionno, it's probably timing if your distributor got f-ed up like that
 

4Jenna

Founding Member
Sep 12, 2001
4,326
6
69
AZ
Jul 11, 2004
#3
  • Jul 11, 2004
  • #3
had the A/C done today lol
I pulled the distrib and everything looks fine...but I had to turn the mofo counter clock wide alot to get it out...tabd were hitting intake...so it was way off I think
 

4Jenna

Founding Member
Sep 12, 2001
4,326
6
69
AZ
Jul 11, 2004
#4
  • Jul 11, 2004
  • #4
 

4Jenna

Founding Member
Sep 12, 2001
4,326
6
69
AZ
Jul 11, 2004
#5
  • Jul 11, 2004
  • #5
 

4Jenna

Founding Member
Sep 12, 2001
4,326
6
69
AZ
Jul 11, 2004
#6
  • Jul 11, 2004
  • #6
 

4Jenna

Founding Member
Sep 12, 2001
4,326
6
69
AZ
Jul 11, 2004
#7
  • Jul 11, 2004
  • #7
And yeas I ran a 11.5@123 and a 11.9@88 with that...lol
 

jacob9

Banned
Jan 20, 2003
86
0
0
los angeles, ca
Jul 11, 2004
#8
  • Jul 11, 2004
  • #8
eades5.0 said:
And yeas I ran a 11.5@123 and a 11.9@88 with that...lol
Click to expand...

i guess its good that it broke. now you can get one of these.

 

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wytstang

Mustang Master
Mar 14, 2004
4,988
4
78
Summerville,SC missing South Fl. weather :(
Jul 11, 2004
#9
  • Jul 11, 2004
  • #9
GEE I wonder why the car felt so slow . Wow you should relace that even if it workes I would change if just for peace of mind b/c that a pretty big peice missing.
 

4Jenna

Founding Member
Sep 12, 2001
4,326
6
69
AZ
Jul 11, 2004
#10
  • Jul 11, 2004
  • #10
LOL yeah!
 

4Jenna

Founding Member
Sep 12, 2001
4,326
6
69
AZ
Jul 11, 2004
#11
  • Jul 11, 2004
  • #11
I got the spare distrib to test and it spins much easier, and doesn't make the rubing noise
Gonna put it in here in a lil bit
 

YEAHLOH95

Founding Member
Nov 19, 2001
1,249
3
39
EVERETT,PA
Jul 11, 2004
#12
  • Jul 11, 2004
  • #12
yeah i when i had my car dynoed it had the stock dist cap and rotor on and the gragh was jumping all over the place up top, so when i blew a head gasket i put the msd dist. in and it helped alot up top i would like to dyno again just to see how much ?hope that fixes your car .
 
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