- Nov 17, 2006
- 38
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Finally got it working! My dad and I took off the plenum, and the bolt that I broke off had a little bit sticking out of the intake. Luckily, it was enough to grab with plyers and pull out, and it wasn't cross threaded at all, so we were able to just get another bolt and fix that. Also, the new gasket I had between the plenum and the intake manifold had a shred in it, (probably from me over tightening it
) so we fixed that also. We took off the fuel rail, cleaned all of the injectors and electrical connectors, and while we were at it replaced all of the spark plugs. Also, one vacuum line was old and ripping at the end, so for now we just cut the end off and put it back on, but I'm going to replace it. Runs like a champ now! Thanks for your help everybody.

The new power curve is great, down low I really don't think I lost much torque, at least it doesn't seem like it, but when I get on it the power is awesome
Pulls right to redline now, I gave it a quick run and it almost felt a little scary. However, aside from a tuner I'm done with these bolt-ons now. I'll save up for the SC 