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Engine 88GT engine rebuild

  • Thread starter Thread starter Pdandy
  • Start date Start date Nov 18, 2019
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Pdandy

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Nov 18, 2019
#1
  • Nov 18, 2019
  • #1
Just picked up this 88 GT with a 347 stroker a few weeks ago.


Seemed to run fine on the test drive and the drive home. But then it started to tick. Thought it was just a lifter that I found was loose. So I reset the lash on it and it was fine for a little bit then started making noise after a short drive. I pulled the intake and found that the spider tray had came loose and allowed a dogbone to jump out of place.



This caused one of the lifters to basically disintegrate and destroy the cam.



I'm pulling the engine this week and will use this thread to update my progress. Any advice is greatly appreciated.
 

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Pdandy

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Nov 18, 2019
#2
  • Nov 18, 2019
  • #2
Got all of the rockers, push rods, and lifters out.

Removed power steering, alternator, drained oil. Getting ready to pull it all out.

 

Blown88GT

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Palm Beach Gardens, FL
Nov 19, 2019
#3
  • Nov 19, 2019
  • #3
Is it your intention to use most of the existing valve train parts?
Keep all the rockers, get a full set of lifters & pushrods & new camshaft?
Looks like the water pump & accessory pulleys are new as are the aftermarket fuel lines & injectors (green top , 42 lb).
New radiator & e-fan, too.

If it's in your budget, I would ditch the OEM 2G alternator which can only output 75A maximum, not enough for an e-fan or even the stock engine with headlamps & fog lamps.
Upgrade to a 3G, which is a very common upgrade; it's almost a drop-in, mechanically; needs larger wire to handle 130A.
BTW, 2G has external fan, 3G has internal fan.

Do not use the fog lamps until you get the electrical sorted out. They will overload the circuit & burn & melt switches & wiring which may already be the case.

I'm seeing quite a few '88's being sold lately.
 
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Pdandy

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Nov 19, 2019
#4
  • Nov 19, 2019
  • #4
Blown88GT said:
Is it your intention to use most of the existing valve train parts?
Keep all the rockers, get a full set of lifters & pushrods & new camshaft?
Looks like the water pump & accessory pulleys are new as are the aftermarket fuel lines & injectors (green top , 42 lb).
New radiator & e-fan, too.

If it's in your budget, I would ditch the OEM 2G alternator which can only output 75A maximum, not enough for an e-fan or even the stock engine with headlamps & fog lamps.
Upgrade to a 3G, which is a very common upgrade; it's almost a drop-in, mechanically; needs larger wire to handle 130A.
BTW, 2G has external fan, 3G has internal fan.

Do not use the fog lamps until you get the electrical sorted out. They will overload the circuit & burn & melt switches & wiring which may already be the case.

I'm seeing quite a few '88's being sold lately.
Click to expand...

I plan on re-using as much as I can. This was a fresh build 5 years ago and has only been driven 200mi since then. The guy who built it only put 100mi on it before selling it and the guy he sold it to only drove it another 100. I suspect they knew something was up with the engine and just didn't care to fix it or didn't know how.

It's funny you mention the alternator. I just watched Dulas video on YouTube on the 3g conversion. That is on my list of things to do.

 

2000xp8

SN Certified Technician
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#5
  • Nov 19, 2019
  • #5
Is that paint on the lifter galley? Not sure that is a place I prefer to paint.

Judging by this post and your other one, the guy who built this had no clue.

Have the heads valve jobbed, at this point with a broken lifter you can't risk putting them back without a professional going through them (it's also worth about 15rwhp).

If it is really a 347, i'd get 30lb injectors and 80mm+ meter calibrated for 30's and pull the chip, you don't need it.
The 3g is a good idea.
I'd also find and reinstall the AC. The only thing removing it does is lower the value of the car. Saves little weight and nets zero hp.
 
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Pdandy

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Nov 19, 2019
#6
  • Nov 19, 2019
  • #6
2000xp8 said:
Is that paint on the lifter galley? Not sure that is a place I prefer to paint.

Judging by this post and your other one, the guy who built this had no clue.

Have the heads valve jobbed, at this point with a broken lifter you can't risk putting them back without a professional going through them (it's also worth about 15rwhp).

If it is really a 347, i'd get 30lb injectors and 80mm+ meter calibrated for 30's and pull the chip, you don't need it.
The 3g is a good idea.
I'd also find and reinstall the AC. The only thing removing it does is lower the value of the car. Saves little weight and nets zero hp.
Click to expand...

The deeper I dig into this, the more I realize he didn't have a clue either. Now I have the chance to do it right.
 
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Pdandy

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#7
  • Nov 19, 2019
  • #7
Anyone want to take bets on whether this is actually a stroker or not?
 

2000xp8

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#8
  • Nov 19, 2019
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I'd bet against.
Kinda why I said "if" it really is.
I really trust no one without hard core proof.
And nothing done to your engine makes any logical sense.
 

Olivethefet

I will own your nuts! LOL
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#9
  • Nov 19, 2019
  • #9
I hope it is a stroker, but I'd bet it isn't.
 

Blown88GT

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Nov 19, 2019
#10
  • Nov 19, 2019
  • #10
2000xp8 said:
...If it is really a 347, i'd get 30lb injectors and 80mm+ meter calibrated for 30's and pull the chip, you don't need it.
The 3g is a good idea.
I'd also find and reinstall the AC. The only thing removing it does is lower the value of the car. Saves little weight and nets zero hp.
Click to expand...
The pic of the injectors indicates they are 42's.
I wrote the "Bible" on the 3G conversion but that website is no more. It's archived here (minus the pictures):
3G 130A ALTERNATOR UPGRADE
 
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Pdandy

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Nov 19, 2019
#11
  • Nov 19, 2019
  • #11
Blown88GT said:
The pic of the injectors indicates they are 42's.
I wrote the "Bible" on the 3G conversion but that website is no more. It's archived here (minus the pictures):
3G 130A ALTERNATOR UPGRADE
Click to expand...

Doing this for sure. I just removed the 2G
 

2000xp8

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#12
  • Nov 19, 2019
  • #12
Blown88GT said:
The pic of the injectors indicates they are 42's.
I wrote the "Bible" on the 3G conversion but that website is no more. It's archived here (minus the pictures):
3G 130A ALTERNATOR UPGRADE
Click to expand...
Yeah, I knew from his other post he had 42's and a stock mass air (I guess there is a first for everything?).
That's why I said replace them with 30's. 42's have no place on any all motor 302 based engine.
If it turns out it's a 302 or 306 he should even go down as low as 24's.

If he wants to tune it after it's all said and works well, I guess he could but a basic hci barely if any benefits from it.
 
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JD1964

there is enough sticking out to grab on to
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#13
  • Nov 19, 2019
  • #13
While you’re at it, deck the block. These sbf’s have a reputation for blowing head gaskets. Need everything perfect. You can buy Cometic mls head gaskets in various thickness to adjust for any material removed by decking the heads and block.

If you imagine yourself being increasingly hungry for more power, build it for boost. You don’t have to boost initially, but its nice to be ready....when you are
 
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Pdandy

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#14
  • Nov 19, 2019
  • #14


It's getting there
 
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Blown88GT

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Nov 20, 2019
#15
  • Nov 20, 2019
  • #15
I think you might have underdrive pulleys. Get rid of them, they are useless & prevent proper cooling.
 

Blown88GT

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Nov 20, 2019
#16
  • Nov 20, 2019
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Pdandy said:
Doing this for sure. I just removed the 2G
Click to expand...
You'll have to clearance the bracket & change the top bolt.
The 3G Alternator Project
 

JD1964

there is enough sticking out to grab on to
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#17
  • Nov 20, 2019
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Car looks like it has a hack wire tuck. I'd be checking all that out and putting things back where they belong.
 
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Steel1

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#18
  • Nov 20, 2019
  • #18
2000xp8 said:
Is that paint on the lifter galley? Not sure that is a place I prefer to paint
Click to expand...
Don't they make some kind of lifter valley paint that is suppose to help with drain back ?
I agree with you though, I would be afraid of paint peeling and clogging things that shouldn't be clogged.
 

General karthief

wonder how much it would cost to ship you a pair
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#19
  • Nov 20, 2019
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I read a lot about painting the lifter valley back in the late 70s early 80s. Never hear about it now.
wonder why. Perhaps?
 
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Pdandy

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#20
  • Nov 20, 2019
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John Dirks Jr said:
Car looks like it has a hack wire tuck. I'd be checking all that out and putting things back where they belong.
Click to expand...

I was just talking to neighbor about that. He's the one helping me pull the engine. I think I'd rather have my windshield wipers back, than have the wire tuck.
 
Last edited: Nov 20, 2019
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