heres an update for the day.
went out to the garage this morning and really got to thinkin about the hood and finally just said screw it and decided id try and get the stocker to work. i had to do some "massaging" to the top of the passenger side valve cover so that the throttle linkage could be hooked up, then i had to trim the throttle linkage bracket so it would clear the valve covers, after that the throttle worked smoothly via the pedal. next i attempted to shut the hood, first i removed the insulation pad then lowered it down slowly, it hit on the breather tube on top of the throttle body so i "massaged" it alittle bit and it cleared so i lowered the hood again and then the drivers side forward corner of the intake hit but the hood was already under the latch and extremely close to being fully closed so i pressed on it slightly and it completely shut, im not willing to grind the corner of the intake since i plan on selling it eventually and going with a different one so im gonna leave it for now.
after i got the hood to shut i decided it was time to take her for a spin, took her off the jack stands, reattached the driveshaft to the rear end with my trusty 12mm and backed her out of the driveway. took her around the block a few times running it through the gears (by the way while it was under the knife i converted it from auto to 5 speed as well) clutch was feelin good, gears shifted fine but was still blowin out a pretty good amount of blueish smoke and was stumbling quite a bit. i brought it back to the house and i reset the base idle once again. afterwards i got brave and took it on a 10 mile loop running through the gears at different rpm's, once i got back to the house this time it was reving from 800-1400rpm back and forth again up and down. she was running pretty decent other then that so i decided to get even braver and i took it on a 90 mile round trip. needless to say for the most part she did very good. i topped off the tank before i left and by the time i was at the halfway point i was already through half the tank which is roughly 6mpg, i turned around and came back and over the same distance going the same speed and same route it used just slightly less then another 1/4 tank which is roughly 11mpg, that tells me the computer must be learning something. also the check engine light was on the entire way there and on the way back it went off. everytime i came to a redlight or a stop sign it would still do the reving thing from about 800-1400 but once i pulled into the driveway the settled on roughly 800-850. it is still blowing some blue smoke at idle but drasticly less then even this morning when i took it around the block.
should i try and do the base idle again or should i just leave it alone and let it learn by itself from here on out?
with it still blowin blue smoke is that tellin me my 42's are too big and i should step down to 30's? or should i go the route of doing the tune to the computer?
when i pulled into the gas station and shut it off i noticed antifreeze coming from the front behind the tire, i raised the hood and it was coming from the drain below where the heater core is. does this mean anything, it hasnt done it since then so
also when i got back after the 90 mile trip i popped the hood and i heard a slight tapping, i made sure my "massaging" of the valve cover wasnt going to interfere with the rockers so i dont think thats it at all. should i pull the valve covers and redo my rockers?
sorry this is so long, had a pretty eventful day
my camera -
http://s121.photobucket.com/albums/o203/badass79cj5/?action=view¤t=MOV03655.flv
wifes camera -
http://s121.photobucket.com/albums/o203/badass79cj5/?action=view¤t=MOV00003.flv