Pulled Codes

Synned

took tubgirl on a date and got banned
Mar 31, 2005
991
1
0
Philly
Okay this is my first time pulling codes and my first time diagnosing problems. I noticed my car felt sluggish so I Pulled codes and got this:

KOEO

33 (rc*): Insufficient EGR flow detected.

15 (o): PCM ROM test failure- failure is internal to PCM. (c) PCM KAM (Keep Alive RAM Memory) failure.

/// IM SCARED ^^


54 (orc*): ACT (Air Charge Temperature)/IAT (Intake Air Temperature) sensor voltage too high, indidcating -40degF. Suspect shorted sensor, harness.

KOER

53 (orc*): TP sensor voltage too high (indicates WOT condition). Suspect shorted TP sensor, harness.

66 (rc*): MAF (2.3 Turbo, VAF) below minimum test voltage.

32 (orc): EVP or PFE voltage below closed limit.


Guys, I have no clue what to do and need all the help I can get. I'm going to clean my MAF and IAC as a start. I don't know what else to do. Please guys...

Thanks.
 
Code 15 - No Keep Alive Memory power to PCM pin 1 or bad PCM (Memory Test Failure). The voltage to the Keep Alive Memory (KAM) is missing (wiring problem) or the KAM is bad. The KAM holds all of the settings that the computer "learns" as it operates and all the stored error codes that are generated as a result of something malfunctioning while the engine is running. Use a voltmeter to check the voltage to the pin 1 on the computer - you should always have 12 volts. No constant 12 volts = bad wiring. If you do always have the 12 volts, then the KAM is bad and the computer is faulty.

Before replacing the computer, remove the battery ground cable for about 20 minutes. This will clear all the codes. Retest after several days of running. If the 15 code is gone, then don't worry about it. If it is still there, then you get to do some troubleshooting.

Wiring diagrams for the proper model years are next…

For 86 models see http://www.autozone.com/images/cds/gif/large/0900823d80167158.gif

For 87 models see http://www.autozone.com/images/cds/gif/large/0900823d8016715e.gif

For 88 models see http://www.autozone.com/images/cds/gif/large/0900823d80167162.gif

For 89-90 models see http://www.autozone.com/images/cds/gif/large/0900823d8019595f.gif

For 91-93 models see http://www.autozone.com/images/cds/gif/large/0900823d80195960.gif

Code 32 - Code 32 – EGR voltage below closed limit

Let’s put on our Inspector Gadget propeller head beanies and think about how this works:
The EGR sensor is a variable resistor with ground on one leg and Vref (5 volts) on the other. Its’ resistance ranges from 4000 to 5500 Ohms measured between Vref & ground, depending on the sensor. The center connection of the variable resistor is the slider that moves in response to the amount of vacuum applied. The slider has some minimum value of resistance greater than 100 ohms so that the computer always sees a voltage present at its’ input. If the value was 0 ohms, there would be no voltage output. Then the computer would not be able to distinguish between a properly functioning sensor and one that had a broken wire or bad connection. The EGR I have in hand reads 700 Ohms between the slider (EPV) and ground (SIG RTN) at rest with no vacuum applied.

As vacuum is applied, the voltage on the slider increases (EVP). As the voltage increases, the computer knows the how much the EGR valve is opened and how much exhaust gas is being recirculated. It uses the load table to calculate the amount of exhaust gas required depending on RPM, Mass Air Flow, ACT, ECT & TPS. It then sends a signal to the Electronic Vacuum Regulator to hold, increase or decrease the vacuum being applied to the EGR valve.

Theory class is over now, let’s spin up our propeller head beanies and get with it… Go Gadget, Go…

Measure the resistance of the EGR sensor between the two end pins. You should see between 3500 to 5500 Ohms. With the sensor removed, measure the resistance again while pressing on the plunger. You should see the resistance drop from its high value to a low reading of 200-700 ohms depending on the sensor. No resistance readings, or values way out of range, the sensor is bad.
If the Orange white wire has Vref, (5 volts =/-.25 volt) then you have some wiring problems because the computer isn’t seeing the minimum voltage on the EVR pin. Ohm the wiring back to the computer. Check for resistance between the brown/lt green wire on the EGR sensor and pin 27 on the computer: you should have less than 1 ohm. Repeat the process for the orange/white wire and pin 26. Do it again between the black/white wire and pin 46. In no case should you have more than 1 ohm. Remember that resistance checks are always done with the power off the circuit.

Code 33 - Insufficient EGR flow detected.
Look for vacuum leaks, cracked vacuum lines, failed EGR vacuum regulator. Check to see if you have 10” of vacuum at the EGR vacuum connection coming from the intake manifold. Look for electrical signal at the vacuum regulator solenoid valves located on the rear of the passenger side wheel well. Using a test light across the electrical connector, it should flicker as the electrical signal flickers. Remember that the computer does not source any power, but provides the ground necessary to complete the circuit. That means one side of the circuit will always be hot, and the other side will go to ground or below 1 volt as the computer switches on that circuit.
Check for resistance between the brown/lt green wire on the EGR sensor and pin 27 on the computer: you should have less than 1 ohm.

See the following website for some help from Tmoss (diagram designer) & Stang&2Birds (website host)

http://www.veryuseful.com/mustang/tech/engine/images/fuel-alt-links-ign-ac.gif

http://www.veryuseful.com/mustang/tech/engine/images/88-91eecPinout.gif


EGR test procedure courtesy of cjones

to check the EGR valve:
bring the engine to normal temp.
connect a vacuum pump to the EGR Valve
apply 5in vacuum to the valve.
if engine stumbled or died then EGR Valve and passage(there is a passageway through the heads and intake) are good.
if engine did NOT stumble or die then either the EGR Valve is bad and/or the passage is blocked.
if engine stumbled, connect vacuum gauge to the hose coming off of the EGR Valve
snap throttle to 2500 RPM (remember snap the throttle don't hold it there).
did the vacuum gauge show about 5in vacuum?

if not, check for manifold vacuum at the EGR vacuum valve.
if you have manifold vacuum then connect vacuum gauge to the EGR valve side of the vacuum valve and snap throttle to 2500 RPM.
should read about 5in vacuum

Code 53 - Throttle Position sensor too high – TPS – TPS out of adjustment, bad connections, missing signal ground, bad sensor.

Here’s a TPS tip I got from NoGo50…

When you installed the sensor make sure you place it on the peg right and then tighten it down properly. Loosen the back screw a tiny bit so the sensor can pivot and loosen the front screw enough so you can move it just a little in very small increments. I wouldn’t try to adjust it using marks. Set it at .97v-.99v, the closer to .99v the better. Just don’t go over .99, or you upset the fuel calibration and idle quality will suffer.

(copied from MustangMax, Glendale AZ)
1. Always adjust the TPS and Idle with the engine at operating temp. Dive it around for a bit if you can and get it nice and warm.

2. When you probe the leads of the TPS, do not use an engine ground, put the ground probe into the lead of the TPS. You should be connecting both meter probes to the TPS and not one to the TPS and the other to ground.

3. Always reset the computer whenever you adjust the TPS or clean/change any sensors. I just pull the battery lead for 10 minutes.

4. Check the procedure for your year, on my 90 I have to turn the idle screw until it just touches the tab, then insert a .010 feeler gauge and give it about one more turn. Then you adjust the TPS voltage to .98v, reset the computer. Start it up, if the idle is to low then turn the screw in until it is just right, then readjust the TPS voltage to .98v and reset the computer and start it up. The key is to adjust the TPS voltage and reset the computer whenever the idle screw is changed.
Check the black/white wire resistance. Connect one ohmmeter lead to the black/white wire on the TPS and one lead to the negative post on the battery. You should see less than .5 ohm, more than that indicates a problem. Always take resistance measurements with the circuit powered off.

Clean the 10 pin salt & pepper shaker connectors.
harness02.gif
.

Code 54 – ACT sensor out of range. Broken or damaged wiring, bad ACT sensor. Note that that if the outside air temp is below 50 degrees F that the test for the ACT can be in error.

Check the resistance of the black/white wire to battery ground. If it is less than 1 ohm, it is good. If it is more than 1 ohm, the black/white wire has bad connections or a broken wire. Always take resistance measurements with the circuit powered off.

Then check the resistance of the ACT sender located in the #5 intake runner on most 5.0 stangs.

ACT & ECT test data:

The ACT & ECT have the same thermistor, so the table values are the same

Pin 7 on the computer - ECT signal in. at 176 degrees F it should be .80 volts

Pin 25 on the computer - ACT signal in. at 50 degrees F it should be 3.5 volts. It is a good number if the ACT is mounted in the inlet airbox. If it is mounted in the lower intake manifold, the voltage readings will be lower because of the heat transfer. Here's the table :

68 degrees F = 3.02 v
86 degrees F = 2.62 v
104 degrees F = 2.16 v
122 degrees F = 1.72 v
140 degrees F = 1.35 v
158 degrees F = 1.04 v
176 degrees F = .80 v
194 degrees F = .61

Ohms measures at the computer with the computer disconnected, or at the sensor with the sensor disconnected.
50 degrees F = 58.75 K ohms
68 degrees F = 37.30 K ohms
86 degrees F = 27.27 K ohms
104 degrees F = 16.15 K ohms
122 degrees F = 10.97 K ohms
140 degrees F = 7.60 K ohms
158 degrees F = 5.37 K ohms
176 degrees F = 3.84 K ohms
194 degrees F = 2.80 K ohms

Code 66 MAF below minimum test voltage.
Insufficient or no voltage from MAF. Dirty MAF element, bad MAF, bad MAF wiring, missing power to MAF. Check for missing +12 volts on this circuit. Check the two links for a wiring diagram to help you find the red wire for computer power relay switched +12 volts. Check for 12 volts between the red and black wires on the MAF heater (usually pins A & B). while the connector is plugged into the MAF. This may require the use of a couple of safety pins to probe the MAF connector from the back side of it.

There are three parts in a MAF: the heater, the sensor element and the amplifier. The heater heats the MAF sensor element causing the resistance to increase. The amplifier buffers the MAF output signal and has a resistor that is laser trimmed to provide an output range compatible with the computer's load tables.

The MAF element is secured by 2 screws & has 1 wiring connector. To clean the element, remove it from the MAF housing and spray it down with electronic parts cleaner or non-inflammable brake parts cleaner (same stuff in a bigger can and cheaper too).

The MAF output varies with RPM which causes the airflow to increase or decease. The increase of air across the MAF sensor element causes it to cool, allowing more voltage to pass and telling the computer to increase the fuel flow. A decrease in airflow causes the MAF sensor element to get warmer, decreasing the voltage and reducing the fuel flow. Measure the MAF output at pins C & D on the MAF connector (dark blue/orange and tan/light blue) or at pins 50 & 9 on the computer.

At idle = approximately .6 volt
20 MPH = approximately 1.10 volt
40 MPH = approximately 1.70 volt
60 MPH = approximately 2.10 volt

Check the resistance of the MAF signal wiring. Pin D on the MAF and pin 50 on the computer (dark blue/orange wire) should be less than 2 ohms. Pin C on the MAF and pin 9 on the computer (tan/light blue wire) should be less than 2 ohms.

There should be a minimum of 10K ohms between either pin C or D on the MAF and ground.

See the following website for some help from Tmoss (diagram designer) & Stang&2Birds (website host)

http://www.veryuseful.com/mustang/tech/engine/images/fuel-alt-links-ign-ac.gif

http://www.veryuseful.com/mustang/tech/engine/images/88-91eecPinout.gif

To clean the MAF, remove the MAF element and gently spray it with electrical contact cleaner. You can also use non-flammable brake parts cleaner (same chemical in a bigger can & cheaper too). Let it dry and put it back in.

http://www.autozone.com/servlet/UiB..._us/0900823d/80/19/59/5a/0900823d8019595a.jsp
 
Thanks jrickter! Does anyone think that these problems have a common source, e.g. one bad wire? Is it common for this many problems to happen on a 52k mile SN95? I don't know if I'll be able to fix all this stuff by myself. I just started to get into this car stuff. Im pretty intimidated.. I don't even know where to start.
 
Synned said:
Is it common for this many problems to happen on a 52k mile SN95?
Your SN should have 3 digit codes. Do you know if someone did a PIH-type conversion? If so, who knows what was done, you know?

Good luck.
 
Are you sure? I thought all mustangs untill OBDII used 2 digit codes. My grandpop owned this mustang before I did, it was 100% stock. I'm almost positive nothing was swapped out.
 
Synned said:
Are you sure? I thought all mustangs untill OBDII used 2 digit codes. My grandpop owned this mustang before I did, it was 100% stock. I'm almost positive nothing was swapped out.
Yep, I am pretty sure. ;)

The processor in 94-95's spit 3 digit codes.

Further non-sequitor info. 94-95's were wired with ports for OBD-I and OBD-II. The V6's in 94 are OBD-II, but 94-95 GT's are OBD-I. The cars have both ALDL's/diagnostic ports though

Something seems a little strange, though I dont doubt the history of your car one bit. You really should have 3 digit codes (further proof: if you consult your repair manual, you should see only 3 digit definitions).