I should add, just in case someone trips across my thread some day in the future. The noid light failed. No light, no injector firing so I went to the 10 pin connector, no power to center pin in black harness. I searched for any wire breaks and did not see anything obvious. I got a needle and poked the green wire on the TPS sensor. Connected alligator clips to my volt meter leads and the needle and a chassis ground screw. 4.4! I loosened 2 screws tried to rotate it, lowest I could get was .92. Fired right up after that! Discovered that my alternator was not charging my battery. Since I did the efan conversion I knew I'd have to upgrade eventually but did not realize it would be right away. Well at least I can pull it back into the garage and work on that and all the millions of other things it needs before it is reliable enough to drive 6 hours to NC! Foxtoberfest or bust!