Hey guys. I'm finally getting a chance to update the progress of my car. Well...I have the fan on a switch that I turn on and off as temps demand. I have it wired through the relay board and its working fine(using 10g wire for everything). Yes, I bought a new relay board. So that takes care of temp control for now.
I since I put the catch can on the car it has to be making at least 75-100 more hp(of course that's a mild exaggeration). Before the catch can if I punched it from a 1st gear roll it wouldn't even spin the tires(M/T drag radials w/ 35psi of air). Now if I punch it from a roll, under those same conditions, except with only 25psi of air in the tires, 1st and half of 2nd gear are useless.....USELESS!!!
So needless to say I've been a little bit of a happy camper lately.

I even went out to play with a couple of my buddies about a week and a half ago. They have faster cars than me but we still had fun. One has a 93 notch with a stroked terminator engine with a Gen2 TVS blower w/ a 6-spd(650rwhp), the other(his twin brother) has a 2015 GT with a Roush blower and many other upgrades and bolt-ons w/ a 6-spd(740rwhp). Yes they pulled away from me but not as hard as I was expecting. My little low compression n/a notch didn't do too bad. Of course the 93 is the fastest of the 3 of us. He has the power:weight advantage.
I finally took my 6 y/o son for a ride in the car today. It scared him a little bit but he had a big smile on his face the whole time.

I since I put the catch can on the car it has to be making at least 75-100 more hp(of course that's a mild exaggeration). Before the catch can if I punched it from a 1st gear roll it wouldn't even spin the tires(M/T drag radials w/ 35psi of air). Now if I punch it from a roll, under those same conditions, except with only 25psi of air in the tires, 1st and half of 2nd gear are useless.....USELESS!!!

So needless to say I've been a little bit of a happy camper lately.


I even went out to play with a couple of my buddies about a week and a half ago. They have faster cars than me but we still had fun. One has a 93 notch with a stroked terminator engine with a Gen2 TVS blower w/ a 6-spd(650rwhp), the other(his twin brother) has a 2015 GT with a Roush blower and many other upgrades and bolt-ons w/ a 6-spd(740rwhp). Yes they pulled away from me but not as hard as I was expecting. My little low compression n/a notch didn't do too bad. Of course the 93 is the fastest of the 3 of us. He has the power:weight advantage.I finally took my 6 y/o son for a ride in the car today. It scared him a little bit but he had a big smile on his face the whole time.


I let the car down onto jack stands under the rearend....still couldn't get the driveshaft back in.
I tried adjusting the UCAs so the rearend could turn down enough to get it in....NOPE! I ended up detaching the UCAs from the rearend and we finally got it in. But there was very little play. After getting everything back together and I test drove the car I have pretty bad high speed(80+ mph) vibration. So I'm thinking the k-member moved toward the rear by maybe 1/4" or so. I'm going to get under the car tomorrow and measure the distance from the tail of the tranny to the face of the pinion yoke. If it's not the same as the measurement I gave American Powertrain for them to make my driveshaft, that will confirm that the k-member moved.
That was the only run I hooked halfway decent, but I short shifted 2nd. So if I would have hooked again the rest of the day I might have pulled off what could have equated to a high 11 at least....which is still disappointing to me. As for what happened at the Da Pad, ice skating. I wish I had video but the video that my buddies wife sent me was really grainy.

